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Table 7 A comparison of the parameters before and after the optimization

From: Influence factor research on deacidification process for high carbon content gas field by numerical simulation—a case study of the Oudeh gas field

Contents

Before optimization

After optimization

Circulation rate of lean solution, m3/h

330

330

flow rate of the wet purified gas, 104Nm3/h

185

184.9

Wet purified gas

H2S, mg/m3

3.7216

4.2562

CO2,  %

2.4359

2.4307

Heat load of reboiler, kW

29,180

28,980

Acid gas load of rich solution, mol/mol

0.5062

0.5006

Electric energy consumption, kWh/d

20,467

19,546

0.4Mpa flow rate of vapor, t/d

927

920

Recycled chilled water, t/d

6415

6402

Supplementary deoxygenation water, t/d

47.4

45.2